The big day is getting closer, and I am pleased to say that my bird is now officially ready for her Airworthiness Condition Inspection, which is scheduled in a couple weeks! All the paperwork has been completed, and everything I can think of has been done to the airplane to make her ready for flight. I'm sure I'll fuss over her a ton, recheck everything, and pitter around over the ensuing days.
I performed several more starts to set the low pitch on the prop to obtain 2650rpm at max throttle, which took only two tries since I read that others had to turn the set screw "in" (clockwise) at least 1.5 turns - mine took exactly 2.5 turns. I also taxied around and checked the brakes - I'm not used to taxiing a castering nosewheel, so it took a couple turns before I got used to the feeling. I'm looking forward to transition training in the factory RV-14A, since this beast is very different from the Cessnas I'm used to flying. Hopefully, the next post will include a picture with my DAR and an aircraft airworthiness certificate. As usual, below and past the break are details from the last two weeks:
- final-drilled #19 holes, deburred, drilled #40 for nutplates; countersunk holes; riveted nutplates; checked prop clearance of gap filler and spinner (and adjusted as necessary); safety-wired 4 bolts that attach forward spinner bulkhead to prop hub
- finished spinner - riveted gap fillers to rear spinner bulkhead (involved removing rear bulkhead to gain access, and retorquing those nuts); sanded aft edge to be flush with bulkhead; checked gaps again and adjusted; safety-wired main wheel pants brackets; torque-striped painted as many nuts/bolts as I could find that were torqued but weren’t striped
- finally fixed the flaps switch! required reversing the flap molex pins at each stick; thanks Ken B. and Glenn M. for making me do this; checked function of autopilot in heading mode (works - goes side to side when the HDG bug is turned); painted seat pans
- worked on the emp. fairing (improved fit, blind-drilled using magnets, up-sized #27, drilled nutplate rivet holes in VS and HS, countersunk #27 holes in fairing)
- deburred holes of emp. fairing, riveted nutplates, attached gap fairings, outlined areas to trim on emp. fairing
- performed second and third run-up; static RPM is now 2650-2660rpm (IAW Hartzell manual, increased fine pitch to reduce top prop. speed); started cleaning plane
- Sanded edges of emp fairing, installed and floxed all “high” areas for better fit; filled fuel tanks with an additional 20gal (approx. 38 gal remaining on board now)
- Removed emp fairing, sanded edges, epoxied inside parts that touch metal; Finished ELT installation, performed ELT self-test, performed yearly ELT function test (between top of the hour and 5min past the hour); installed Canopy Hinge covers; installed database updates
- Taxi and brake test and mag ground check (Hobbs: 0.5h; Tach 0.3h); added W&B to G3X; applied 3M 2000+ degree fire barrier to firewall pass-throughs; attached crotch seatbelt straps; finished initial Condition Inspection and wrote the certification statement in my logbook. The airplane is ready for the Airworthiness Condition Inspection (although I’m sure I’ll still fuss over it)